W DOC AIRBUS | TSM A320F

Failure of the Control of the Fuel Shut-off Valve on Engine 1


TASK 76-12-00-810-814-A
Failure of the Control of the Fuel Shut-off Valve on Engine 1


1. Possible Causes
  • HMU
  • aircraft wiring
  • CTL SW-ENG/MASTER 1 [3KC]
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
ESPM 2045210
AMM 31-10-00-700-001
Test Program after Removal/Installation of a VU panel
AMM 71-00-00-710-003
Engine Automatic Start
AMM 73-21-10-000-001
Removal of the Hydromechanical Unit (HMU)
AMM 73-21-10-000-002
Removal of the Hydromechanical Unit (HMU)
AMM 73-21-10-400-001
Installation of the Hydromechanical Unit (HMU)
AMM 73-21-10-400-002
Installation of the Hydromechanical Unit (HMU)
ASM 761201
AWM 761201
3. Fault Confirmation
Subtask 76-12-00-710-074-A ** ON A/C NOT FOR ALL
A. Test
   (1) Not applicable, the fault is evident.
4. Fault Isolation
Subtask 76-12-00-865-054-A ** ON A/C NOT FOR ALL
A. Table of the circuit breakers used in this procedure:
PANELDESIGNATIONFINLOCATION
** ON A/C NOT FOR ALL
49VUENGINE/1/HP FUEL SOV1KC1A01
Subtask 76-12-00-810-062-B ** ON A/C NOT FOR ALL
B. If the fault symptom is identified by the CFDS message MASTER LEVER, HMU:
NOTE: The fault is generated if there is a demand / position disagree on the HMU HP fuel shut-off valve. While the A/C is electrically powered and the engine master lever is set to OFF.
  • disconnect the connector 4000KC-A from the HMU and make sure that, when the ENG/MASTER control switch on the 115VU is in the OFF position, there is 28VDC at pin AA/1 of the connector 4000KC-A ASM 761201 and AWM 761201.
   (1) If there is 28VDC:
   (2) If there is no 28VDC:
  • remove the panel 115VU.
  • do a check of the aircraft wiring between the connector 4000KC-A and the ENG/MASTER control switch (3KC) pin AA/1 to pin 1G.
  • do a check of the aircraft wiring between the ENG/MASTER control switch (3KC) pin 3G and the circuit breaker (1KC1) ASM 761201.
     (a) If the wiring is not correct:
  • repair the above defective wirings.
     (b) If the wiring is correct:
Subtask 76-12-00-810-062-C ** ON A/C NOT FOR ALL
B. If the fault symptom is identified by the CFDS message MASTER LEVER, HMU:
NOTE: The fault is generated if there is a demand / position disagree on the HMU HP fuel shut-off valve. While the A/C is electrically powered and the engine master lever is set to OFF.
  • disconnect the connector 4000KC-A from the HMU and make sure that, when the ENG/MASTER control switch on the 115VU is in the OFF position, there is 28VDC at pin AA/1 of the connector 4000KC-A ASM 761201 and AWM 761201.
   (1) If there is 28VDC:
   (2) If there is no 28VDC:
  • remove the panel 115VU.
  • do a check of the aircraft wiring between the connector 4000KC-A and the ENG/MASTER control switch (3KC) pin AA/1 to pin 1G.
  • do a check of the aircraft wiring between the ENG/MASTER control switch (3KC) pin 3G and the circuit breaker (1KC1) ASM 761201.
     (a) If the wiring is not correct:
  • repair the above defective wirings.
     (b) If the wiring is correct:
Subtask 76-12-00-710-075-A ** ON A/C NOT FOR ALL
C. Test
   (1) Start the engine 1 by the engine automatic start procedure AMM 71-00-00-710-003.
   (2) Make sure that there is no ECAM and CFDS fault message shown.
[Rev.8 from Aug 2018] 2026.04.04 04:37:27 UTC