W DOC AIRBUS | TSM A320F

EIU-2 Relay Fault for Hydraulic Pump Depressurization


TASK 73-25-00-810-A51-A
EIU-2 Relay Fault for Hydraulic Pump Depressurization


1. Possible Causes
  • EIU-2 [1KS2]
  • PUMP VARIABLE DTS [3030GD]
  • HARNESS-IDG, ENG PUMP AND LOW OIL PRESS SW [4155KS]
  • aircraft wiring
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
AWM 291301
AMM 29-13-51-000-806
Removal of the Yellow Engine Driven Pump
AMM 29-13-51-400-806
Installation of the Yellow Engine Driven Pump
AMM 71-13-00-410-802
Closing of the Fan Cowl Doors
AMM 71-51-40-000-801
Removal of the IDG-EDP-MON Harness
AMM 71-51-40-400-801
Installation of the IDG-EDP-MON Harness
AMM 73-25-34-000-802
Removal of the Engine Interface Unit (EIU)
AMM 73-25-34-400-802
Installation of the Engine Interface Unit (EIU)
AMM 73-25-34-710-802
Operational Test of the Engine Interface Unit (EIU) with the Centralized Fault Display System (CFDS)
AMM 78-36-00-010-802
Opening of the Thrust Reverser Cowl-Doors
3. Fault Confirmation
Subtask 73-25-00-710-488-A ** ON A/C NOT FOR ALL
A. Do the operational test of the Engine Interface Unit (EIU) with the Centralized Fault Display System (CFDS) to confirm this fault AMM 73-25-34-710-802.
4. Fault Isolation
Subtask 73-25-00-810-332-A ** ON A/C NOT FOR ALL
A. If there is confirmation of the fault:
   (1) Replace EIU-2 [1KS2] AMM 73-25-34-000-802 and AMM 73-25-34-400-802.
     (a) Do the test given in Para. 3.
   (2) If the fault continues:
     (a) On HYD/Fuel panel 40VU, make sure that the pushbutton switch (3703GD) is released (OFF legend is off).
   (3) Remove EIU-2 [1KS2] AMM 73-25-34-000-802.
   (4) Open the right thrust reverser cowl-door AMM 78-36-00-010-802.
   (5) Remove connector (3030GD-A) from the hydraulic engine pump.
   (6) Put a shunt between pins 1 and 3 of connector (3030GD-A)
   (7) On shelf 86VU, check for a ground at pin 15J of connector AB at rack side.
     (a) If you find a ground:
       1 Replace PUMP VARIABLE DTS [3030GD] AMM 29-13-51-000-806 and AMM 29-13-51-400-806.
       2 Do the test given in Para. 3.
   (8) If you do not find a ground:
     (a) Remove the shunt.
     (b) Remove connector (404VC2-A) from the pylon junction box.
     (c) Examine the pins and sockets (contacts) for alignment and damage. Look for contacts pushed rearward into both connectors face. Replace parts as necessary.
     (d) If you find damage:
       1 Do the test given in Para. 3.
   (9) If you find no damage to connectors or if the fault continues, put a shunt between pins 22 and 23 of connector (404VC2).
   (10) On shelf 86VU, check for a ground at pin 15J of connector AB at rack side.
     (a) Remove the shunt.
     (b) If you find a ground:
       1 Replace HARNESS-IDG, ENG PUMP AND LOW OIL PRESS SW [4155KS] AMM 71-51-40-000-801 and AMM 71-51-40-400-801.
       2 Do the test given in Para. 3.
   (11) If you do not find a ground:
     (a) Repair or replace aircraft wiring AWM 291301.
     (b) Do the test given in Para. 3.
5. Close-up
Subtask 73-25-00-860-093-A ** ON A/C NOT FOR ALL
A. Put the aircraft back to its initial configuration.
   (1) Make sure that the work area is clean and clear of tools and other items.
     (a) Close the fan cowl doors AMM 71-13-00-410-802.
[Rev.8 from Aug 2018] 2026.04.04 04:36:29 UTC