EIU-2 Position Fault
TASK 73-25-00-810-A47-A
EIU-2 Position Fault
1. Possible Causes
A. Referenced Information
3. Fault Confirmation
Subtask 73-25-00-710-484-A ** ON A/C NOT FOR ALL
Subtask 73-25-00-810-328-A ** ON A/C NOT FOR ALL
[Rev.8 from Aug 2018]
2026.04.04 04:36:29 UTC
EIU-2 Position Fault
1. Possible Causes
- aircraft wiring
- EIU-2 [1KS2]
A. Referenced Information
| REFERENCE | DESIGNATION |
|---|---|
| AWM 732504 | |
| AMM 73-25-34-000-802 | Removal of the Engine Interface Unit (EIU) |
| AMM 73-25-34-400-802 | Installation of the Engine Interface Unit (EIU) |
| AMM 73-25-34-710-802 | Operational Test of the Engine Interface Unit (EIU) with the Centralized Fault Display System (CFDS) |
| AMM 73-25-34-860-806 | Engine Interface Unit (EIU) DISCRETE INPUTS Menu Data Status |
Subtask 73-25-00-710-484-A ** ON A/C NOT FOR ALL
A. Do the operational test of the Engine Interface Unit (EIU) with the Centralized Fault Display System (CFDS) to confirm this fault AMM 73-25-34-710-802.
4. Fault IsolationSubtask 73-25-00-810-328-A ** ON A/C NOT FOR ALL
A. If there is confirmation of the fault:
(1) Check the status of EIU-2 discrete input for ENGINE 1 and ENGINE 2 AMM 73-25-34-860-806.
(a) Check the status of ENGINE 2 is 1 and the status of ENGINE 1 is 0.
(b) If the status of ENGINE 2 is not 1:
1 Repair or replace aircraft wiring to have the pin 4B of connector AA at ground AWM 732504.
(c) If the status of ENGINE 1 is not 0:
1 Repair aircraft wiring to have the pin 3A of connector AA unused AWM 732504.
(d) Do the test given in Para. 3.
(2) If both statuses are correct or if the fault continues:
(a) Replace EIU-2 [1KS2] AMM 73-25-34-000-802 and AMM 73-25-34-400-802.
(1) Check the status of EIU-2 discrete input for ENGINE 1 and ENGINE 2 AMM 73-25-34-860-806.
(a) Check the status of ENGINE 2 is 1 and the status of ENGINE 1 is 0.
(b) If the status of ENGINE 2 is not 1:
1 Repair or replace aircraft wiring to have the pin 4B of connector AA at ground AWM 732504.
(c) If the status of ENGINE 1 is not 0:
1 Repair aircraft wiring to have the pin 3A of connector AA unused AWM 732504.
(d) Do the test given in Para. 3.
(2) If both statuses are correct or if the fault continues:
(a) Replace EIU-2 [1KS2] AMM 73-25-34-000-802 and AMM 73-25-34-400-802.