W DOC AIRBUS | TSM A320F

Loss of the 28VDC Power Supply of the ECU on the Engine 2


TASK 73-25-00-810-947-A
Loss of the 28VDC Power Supply of the ECU on the Engine 2


1. Possible Causes
  • EIU-2 [1KS2]
  • ECU [4000KS]
  • aircraft wiring
  • C/B-ENGINE/ENG2/FADEC B/AND EIU 2 [4KS2]
  • harness J2
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
AMM 73-21-60-000-001
Removal of the Electronic Control Unit (ECU)
AMM 73-21-60-400-001
Installation of the Electronic Control Unit (ECU)
ASM 732505
ASM 732508
AMM 73-25-34-000-040
Removal of the Engine Interface Unit (EIU)
AMM 73-25-34-400-040
Installation of the Engine Interface Unit (EIU)
AMM 73-29-00-710-040
Operational Test of the FADEC on the ground (with Engine Motoring)
3. Fault Confirmation
Subtask 73-25-00-865-055-A ** ON A/C NOT FOR ALL
A. Make sure that this(these) circuit breaker(s) is(are) closed:
PANELDESIGNATIONFINLOCATION
** ON A/C NOT FOR ALL
121VUENGINE/ENG2/FADEC B/AND EIU 24KS2Q40
Subtask 73-25-00-710-341-A ** ON A/C NOT FOR ALL
B. Test
   (1) Do the operational test of the FADEC 2B on the ground (with engine motoring) AMM 73-29-00-710-040.
   (2) If the circuit breaker (4KS2) is open, refer to Para. 4.A.(2).
4. Fault Isolation
Subtask 73-25-00-810-199-A ** ON A/C NOT FOR ALL
A. If the test gives the maintenance message EIU - 28V, ECU:
  • do a check of the status of the circuit breaker (4KS2).
   (1) If the circuit breaker is closed:
  • disconnect the connector J2 from the ECU (4000KS) and do a check for 28VDC at pin J2/13 with the FADEC GND PWR pushbutton switch released (the ON legend is on) ASM 732505.
     (a) If there is 28VDC:
     (b) If there is no 28VDC:
  • do a check for 28VDC at EIU 2 (1KS2) pin AC/9 ASM 732505.
       1 If there is no 28VDC:
  • do a check for open or short to ground at the aircraft wiring from the circuit breaker (4KS2) to EIU 2 (1KS2) pins AC/9.
         a If there is a short to ground:
  • repair the above wiring.
         b If there is no short to ground:
  • replace the C/B-ENGINE/ENG2/FADEC B/AND EIU 2 [4KS2] .
       2 If there is 28VDC:
  • do a check for open or short to ground at the harness J2 between the EIU 2 (1KS2) and the ECU (4000KS), pin AC/2 to pin J2/13. Replace the harness J2 if necessary ASM 732505.
       3 If the fault continues:
  • make sure that there is no ground signal at EIU 2 (1KS2) pin AA/5B ASM 732508.
     (c) If the fault continues:
   (2) If the circuit breaker (4KS2) is open:
  • close the circuit breaker.
     (a) If the circuit breaker trips:
     (b) If the fault continues:
  • do a check for a short to ground at the harness J2 between the EIU 2 (1KS2) and the ECU (4000KS), pin AC/2 to pin J2/13.
       1 If there is a short to ground:
  • replace the harness J2 .
       2 If there is no short to ground:
  • do a check for a short to ground at the aircraft wiring between EIU 2 (1KS2) pin AC/9 and the circuit breaker (4KS2).
         a If there is a short to ground:
  • repair the above wiring.
         b If there is no short to ground:
  • replace the C/B-ENGINE/ENG2/FADEC B/AND EIU 2 [4KS2] .
Subtask 73-25-00-710-342-A ** ON A/C NOT FOR ALL
B. Do the test given in Para. 3.B.
[Rev.8 from Aug 2018] 2026.04.04 04:35:51 UTC