Loss of the 28VDC Power Supply of the ECU on the Engine 1
TASK 73-25-00-810-909-A
Loss of the 28VDC Power Supply of the ECU on the Engine 1
1. Possible Causes
A. Referenced Information
3. Fault Confirmation
Subtask 73-25-00-865-052-A ** ON A/C NOT FOR ALL
Subtask 73-25-00-810-160-A ** ON A/C NOT FOR ALL
[Rev.8 from Aug 2018]
2026.04.04 04:35:48 UTC
Loss of the 28VDC Power Supply of the ECU on the Engine 1
1. Possible Causes
- EIU-1 [1KS1]
- ECU [4000KS]
- aircraft wiring
- C/B-ENGINE/1/FADEC A/AND EIU 1 [2KS1]
- harness J1
- harness J1
A. Referenced Information
| REFERENCE | DESIGNATION |
|---|---|
| AMM 73-21-60-000-001 | Removal of the Electronic Control Unit (ECU) |
| AMM 73-21-60-400-001 | Installation of the Electronic Control Unit (ECU) |
| ASM 732505 | |
| ASM 732508 | |
| AMM 73-25-34-000-040 | Removal of the Engine Interface Unit (EIU) |
| AMM 73-25-34-400-040 | Installation of the Engine Interface Unit (EIU) |
| AMM 73-29-00-710-040 | Operational Test of the FADEC on the ground (with Engine Motoring) |
Subtask 73-25-00-865-052-A ** ON A/C NOT FOR ALL
A. Make sure that this(these) circuit breaker(s) is(are) closed:
Subtask 73-25-00-710-268-A ** ON A/C NOT FOR ALL | PANEL | DESIGNATION | FIN | LOCATION |
|---|---|---|---|
| ** ON A/C NOT FOR ALL | |||
| 49VU | ENGINE/1/FADEC A/AND EIU 1 | 2KS1 | A04 |
B. Test
(1) If the circuit breaker (2KS1) is open, refer to Para. 4.A.(2).
(2) Do the operational test of the FADEC 1A on the ground (with engine motoring) AMM 73-29-00-710-040.
4. Fault Isolation(1) If the circuit breaker (2KS1) is open, refer to Para. 4.A.(2).
(2) Do the operational test of the FADEC 1A on the ground (with engine motoring) AMM 73-29-00-710-040.
Subtask 73-25-00-810-160-A ** ON A/C NOT FOR ALL
A. If the test gives the maintenance message EIU - 28V, ECU:
Subtask 73-25-00-710-269-A ** ON A/C NOT FOR ALL - do a check of the status of the circuit breaker (2KS1).
- disconnect the connector J1 from the ECU (4000KS) and do a check for 28VDC at pins J1/13 with the FADEC GND PWR pushbutton switch released (the ON legend is on) ASM 732505.
- replace the EIU-1 [1KS1] (the most possible failure is the EIU 28V relay) AMM 73-25-34-000-040 and AMM 73-25-34-400-040
- replace the ECU [4000KS] (the most possible failure is an ECU diode) AMM 73-21-60-000-001 and AMM 73-21-60-400-001.
- do a check for 28VDC at EIU 1 (1KS1) pin AC/11 ASM 732505.
- do a check for open or short to ground at the aircraft wiring from the circuit breaker (2KS1) to EIU 1 (1KS1) pin AC/11.
- repair the above wiring.
- replace the C/B-ENGINE/1/FADEC A/AND EIU 1 [2KS1] .
- do a check for open or short to ground at the harness J1 between the EIU 1 (1KS1) and the ECU (4000KS), pin AC/7 to pin J1/13. Replace the harness J1 if necessary ASM 732505.
- make sure that there is no ground signal at EIU 1 (1KS1) pin AA/5B ASM 732508.
- replace the EIU-1 [1KS1] AMM 73-25-34-000-040 and AMM 73-25-34-400-040.
- close the circuit breaker.
- replace the EIU-1 [1KS1] AMM 73-25-34-000-040 and AMM 73-25-34-400-040
- replace the ECU [4000KS] AMM 73-21-60-000-001 and AMM 73-21-60-400-001.
- do a check for a short to ground at the harness J1 between the EIU 1 (1KS1) and the ECU (4000KS), pin AC/7 to pin J1/13.
- replace the harness J1 .
- do a check for a short to ground at the aircraft wiring between EIU 1 (1KS1) pins AC/11 and the circuit breaker (2KS1).
- repair the above wiring.
- replace the C/B-ENGINE/1/FADEC A/AND EIU 1 [2KS1] .
B. Do the test given in Para. 3.B.