W DOC AIRBUS | TSM A320F

Low Bleed Temperature of ENG 2 in Descent


TASK 36-11-00-810-A46-A
Low Bleed Temperature of ENG 2 in Descent


1. Possible Causes
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
AMM 36-11-00-740-802
BITE Test of the Engine Bleed Air System (EBAS) (System Test)
ASM 361102
AMM 36-11-17-000-001
Removal of the Heat-Exchanger Outlet-Temperature Sensor
AMM 36-11-17-400-001
Installation of the Heat-Exchanger Outlet-Temperature Sensor
AMM 36-11-51-000-802
Removal of the HP Bleed Valve
AMM 36-11-51-400-802
Installation of the HP Bleed Valve
3. Fault Confirmation
Subtask 36-11-00-710-519-A ** ON A/C NOT FOR ALL
A. Test
   (1) Do the BITE test EBAS AMM 36-11-00-740-802.
4. Fault Isolation
Subtask 36-11-00-810-503-A ** ON A/C NOT FOR ALL
A. If the BITE test gives no maintenance message:
  • No maintenance is necessary.
   (1) If the BITE test gives the class 3 maintenance message:
TEMP SENSOR 6HA2
Subtask 36-11-00-810-535-A ** ON A/C NOT FOR ALL
B. If the fault continues:
   (1) Do a check and repair the wiring ASM 361102 between:
  • Engine 2 Exchanger Output Temperature Sensor (6HA2) pin A/1 and pin A/2 and BMC 2 (1HA2) pin AA/2C and pin AA/2B.
  • Engine 2 Exchanger Output Temperature Sensor (6HA2) pin B/1 and pin B/2 and BMC 2 (1HA2) pin AB/7D and pin AB/7E.
   (2) If the BITE test gives the class 3 maintenance message:
HP BLEED-V 4000HA2
Subtask 36-11-00-710-520-A ** ON A/C NOT FOR ALL
C. After the subsequent flight, make sure that the fault does not continue.
[Rev.8 from Aug 2018] 2026.04.04 04:33:58 UTC