W DOC AIRBUS | TSM A320F

Low Bleed Temperature of Engine 1 in Climb


TASK 36-11-00-810-A41-A
Low Bleed Temperature of Engine 1 in Climb


1. Possible Causes
  • SENSOR-EXCHANGER OUT TEMP, ENG 1 [6HA1]
  • wiring
  • VALVE-FAN AIR, ENG1 [7120HM1]
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
AMM 36-11-00-740-802
BITE Test of the Engine Bleed Air System (EBAS) (System Test)
ASM 361101
AMM 36-11-17-000-001
Removal of the Heat-Exchanger Outlet-Temperature Sensor
AMM 36-11-17-400-001
Installation of the Heat-Exchanger Outlet-Temperature Sensor
AMM 36-11-54-000-803
Removal of the Fan Air Valve (FAV)
AMM 36-11-54-400-803
Installation of the Fan Air Valve (FAV)
AMM 36-11-54-720-804
Functional Test of the Opening of the Fan Air Valve with the Bleed Test Set P/N 98D36109001000
3. Fault Confirmation
Subtask 36-11-00-710-509-A ** ON A/C NOT FOR ALL
A. Test
   (1) Do the BITE test EBAS AMM 36-11-00-740-802.
4. Fault Isolation
Subtask 36-11-00-810-498-A ** ON A/C NOT FOR ALL
A. If the BITE test gives the class 3 maintenance message:
TEMP SENSOR 6HA1
   (1) Replace the SENSOR-EXCHANGER OUT TEMP, ENG 1 [6HA1] AMM 36-11-17-000-001 and AMM 36-11-17-400-001.
Subtask 36-11-00-810-510-A ** ON A/C NOT FOR ALL
B. If the fault continues:
   (1) Do a check of the wiring ASM 361101 between:
  • Engine 1 Exchanger Output Temperature Sensor (6HA1) pin B/1 and pin B/2 and BMC 1 (1HA1) pin AA/2C and pin AA/2B.
  • Engine 1 Exchanger Output Temperature Sensor (6HA1) pin A/1 and pin A/2 and BMC 1 (1HA1) pin AA/7D and pin AA/7E.
     (a) If the wiring is not correct:
  • Repair or replace the wiring .
     (b) If the wiring is correct:
       1 Do a functional test of the fan air valve AMM 36-11-54-720-804.
         a If the test is not OK:
Subtask 36-11-00-710-510-A ** ON A/C NOT FOR ALL
C. After the subsequent flight, make sure that the fault does not continue.
[Rev.8 from Aug 2018] 2026.04.04 04:33:58 UTC