W DOC AIRBUS | TSM A320F

Low Bleed Pressure of the Engine 2 in Cruise


TASK 36-11-00-810-A32-A
Low Bleed Pressure of the Engine 2 in Cruise


1. Possible Causes
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
AMM 36-11-00-740-802
BITE Test of the Engine Bleed Air System (EBAS) (System Test)
AMM 36-11-16-000-802
Removal of the Bleed Regulated Pressure-Transducer
AMM 36-11-16-400-802
Installation of the Bleed Regulated Pressure-Transducer
AMM 36-11-16-720-802
Functional Test of the Bleed Regulated Pressure-Transducer with the Bleed Test Set P/N 98D36109001000
AMM 36-11-51-000-802
Removal of the HP Bleed Valve
AMM 36-11-51-400-802
Installation of the HP Bleed Valve
AMM 36-11-51-720-804
Functional Test of the HP Bleed Valve with the Test Set P/N 98D36109001000
AMM 36-11-52-000-802
Removal of the Bleed Pressure-Regulator Valve
AMM 36-11-52-400-802
Installation of the Bleed Pressure-Regulator Valve
AMM 36-11-52-720-811
Functional Test of the Pressure Regulator Valve with the Test Set P/N 98D36109001000
3. Fault Confirmation
Subtask 36-11-00-710-491-A ** ON A/C NOT FOR ALL
A. Test
   (1) Do the BITE test of the EBAS AMM 36-11-00-740-802.
4. Fault Isolation
Subtask 36-11-00-810-486-A ** ON A/C NOT FOR ALL
A. If the test gives a maintenance message:
  • Do the trouble shooting procedure related to the maintenance message.
   (1) If there is no maintenance message:
     (a) Do a functional test of the bleed valve AMM 36-11-52-720-811.
       1 If the test is not OK:
Subtask 36-11-00-810-508-A ** ON A/C NOT FOR ALL
B. If the fault continues:
   (1) Do a functional test of the bleed pressure sensor AMM 36-11-16-720-802.
   (2) If the test is not OK:
Subtask 36-11-00-810-509-A ** ON A/C NOT FOR ALL
C. If the fault continues:
   (1) Do a functional test of the HP bleed valve AMM 36-11-51-720-804.
     (a) If the test is not OK:
Subtask 36-11-00-710-492-A ** ON A/C NOT FOR ALL
D. After the subsequent flight, make sure that the fault does not continue.
[Rev.8 from Aug 2018] 2026.04.04 04:33:57 UTC