High Bleed Pressure of the Engine 1 in Cruise
TASK 36-11-00-810-A23-A
High Bleed Pressure of the Engine 1 in Cruise
1. Possible Causes
2. Job Set-up Information
A. Referenced Information
3. Fault Confirmation
Subtask 36-11-00-710-474-A ** ON A/C NOT FOR ALL 4. Fault Isolation
Subtask 36-11-00-810-477-A ** ON A/C NOT FOR ALL
[Rev.8 from Aug 2018]
2026.04.04 04:33:57 UTC
High Bleed Pressure of the Engine 1 in Cruise
1. Possible Causes
2. Job Set-up Information
A. Referenced Information
| REFERENCE | DESIGNATION |
|---|---|
| AMM 36-11-00-740-802 | BITE Test of the Engine Bleed Air System (EBAS) (System Test) |
| AMM 36-11-16-000-802 | Removal of the Bleed Regulated Pressure-Transducer |
| AMM 36-11-16-400-802 | Installation of the Bleed Regulated Pressure-Transducer |
| AMM 36-11-16-720-802 | Functional Test of the Bleed Regulated Pressure-Transducer with the Bleed Test Set P/N 98D36109001000 |
| AMM 36-11-51-000-802 | Removal of the HP Bleed Valve |
| AMM 36-11-51-400-802 | Installation of the HP Bleed Valve |
| AMM 36-11-51-720-804 | Functional Test of the HP Bleed Valve with the Test Set P/N 98D36109001000 |
Subtask 36-11-00-710-474-A ** ON A/C NOT FOR ALL 4. Fault Isolation
Subtask 36-11-00-810-477-A ** ON A/C NOT FOR ALL
A. If the test gives a maintenance message:
(a) If there is no maintenance message:
Subtask 36-11-00-810-519-A ** ON A/C NOT FOR ALL - Do the trouble shooting procedure related to the maintenance message.
(a) If there is no maintenance message:
- Replace the
[4000HA] AMM 36-11-51-000-802 and AMM 36-11-51-400-802.
B. If the fault continues:
(1) Do a functional test of the BPS AMM 36-11-16-720-802.
(2) Replace the XDCR-BLEED REGULATED PRESS, ENG 1 [8HA1] AMM 36-11-16-000-802 and AMM 36-11-16-400-802.
Subtask 36-11-00-710-475-A ** ON A/C NOT FOR ALL (1) Do a functional test of the BPS AMM 36-11-16-720-802.
(2) Replace the XDCR-BLEED REGULATED PRESS, ENG 1 [8HA1] AMM 36-11-16-000-802 and AMM 36-11-16-400-802.
C. After the subsequent flight, make sure that the fault does not continue.