W DOC AIRBUS | TSM A320F

Engine 1 Differental Pressure Transducer Drift Measurement


TASK 36-11-00-810-A19-A
Engine 1 Differental Pressure Transducer Drift Measurement


1. Possible Causes
  • XDCR-BLEED DIFFERENTIAL PRESS, ENG1 [18HA1]
  • sense line
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
AMM 36-11-00-740-805
Drift Test of the Pressure Sensor
AMM 36-11-18-000-801
Removal of the Bleed Differential Pressure-Transducer
AMM 36-11-18-400-801
Installation of the Bleed Differential Pressure-Transducer
AMM 36-11-49-000-826
Removal of the Sense Line between the Bleed-Air Precooler Exchanger (Upstream) and the Bleed Differential Pressure-Transducer
AMM 36-11-49-400-826
Installation of the Sense Line between the Bleed-Air Precooler Exchanger (Upstream) and the Bleed Differential Pressure-Transducer
AMM 36-12-00-860-802
Pressurization of the Bleed System with the APU
AMM 36-12-00-860-803
Pressurization of the Bleed System through the HP Ground Connector
AMM 36-22-00-790-802
Leak Check on all the Bleed Air Ducts and Packs Components
3. Fault Confirmation
Subtask 36-11-00-740-113-A ** ON A/C NOT FOR ALL
A. Test
   (1) Pressurize the Bleed Air System AMM 36-12-00-860-802 or AMM 36-12-00-860-803
   (2) Do the Pressure Sensor Drift Test AMM 36-11-00-740-805
4. Fault Isolation
Subtask 36-11-00-810-459-A ** ON A/C NOT FOR ALL
A. If the test shows the maintenance message:
DRIFT DIFF-PRESS XDCR (18HA1)/ SENSE LINE
   (1) Replace the XDCR-BLEED DIFFERENTIAL PRESS, ENG1 [18HA1] AMM 36-11-18-000-801 and AMM 36-11-18-400-801.
   (2) Do the test given in Para. 3.
Subtask 36-11-00-810-460-A ** ON A/C NOT FOR ALL
B. If the fault continues:
   (1) Replace the sense line of the bleed differential pressure-transducer AMM 36-11-49-000-826 and AMM 36-11-49-400-826.
   (2) Do a leak check of the sense line AMM 36-22-00-790-802.
Subtask 36-11-00-710-649-A ** ON A/C NOT FOR ALL
C. Test
   (1) After the subsequent flight, make sure that the fault does not continue.
[Rev.8 from Aug 2018] 2026.04.04 04:33:56 UTC