W DOC AIRBUS | TSM A320F

Engine 2 Bleed Manifold Pressure Sensor Drift Measurement


TASK 36-11-00-810-A17-A
Engine 2 Bleed Manifold Pressure Sensor Drift Measurement


1. Possible Causes
  • XDCR-BLEED TRANSFER PRESS, ENG 2 [7HA2]
  • sense line
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
AMM 36-11-15-000-802
Removal of the Bleed Transferred Pressure-Transducer
AMM 36-11-15-400-802
Installation of the Bleed Transferred Pressure-Transducer
AMM 36-11-49-000-823
Removal of the Environmental Control System (ECS) Sense Lines
AMM 36-11-49-000-832
Removal of the Sense Lines of the Bleed Regulated Pressure-Transducer and the Bleed Transferred Pressure-Transducer
AMM 36-11-49-400-823
Installation of the Environmental Control System (ECS) Sense Lines
AMM 36-11-49-400-832
Installation of the Sense Lines of the Bleed Regulated Pressure-Transducer and the Bleed Transferred Pressure-Transducer
AMM 36-22-00-790-802
Leak Check on all the Bleed Air Ducts and Packs Components
3. Fault Confirmation
Subtask 36-11-00-740-111-A ** ON A/C NOT FOR ALL
A. Not applicable
4. Fault Isolation
Subtask 36-11-00-810-449-A ** ON A/C NOT FOR ALL
A. If the test shows the maintenance message:
DRIFT TRANSF-PRESS XDCR(7HA2)/ SENSE LINE
   (1) Replace the XDCR-BLEED TRANSFER PRESS, ENG 2 [7HA2] AMM 36-11-15-000-802 and AMM 36-11-15-400-802.
   (2) Do the test given in Para. 3.
Subtask 36-11-00-810-450-A ** ON A/C NOT FOR ALL
B. If the fault continues:
   (1) Replace the sense line of the bleed transferred pressure-transducer AMM 36-11-49-000-823 AMM 36-11-49-400-823 and AMM 36-11-49-000-832 AMM 36-11-49-400-832.
   (2) Do a leak check of the sense line AMM 36-22-00-790-802.
Subtask 36-11-00-710-647-A ** ON A/C NOT FOR ALL
C. Test
   (1) After the subsequent flight, make sure that the fault does not continue.
[Rev.8 from Aug 2018] 2026.04.04 04:33:56 UTC