W DOC AIRBUS | TSM A320F

High Pressure Valve of Engine 1 Failed in Close Position


TASK 36-11-00-810-973-A
High Pressure Valve of Engine 1 Failed in Close Position


1. Possible Causes
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
ASM 361101
AMM 36-11-41-000-802
Removal of the Intermediate-Pressure Bleed Check-Valve
AMM 36-11-41-200-802
Removal of Intermediate Pressure Bleed Check Valve for Detailed Inspection
AMM 36-11-41-400-802
Installation of the Intermediate-Pressure Bleed Check-Valve
AMM 36-11-51-000-802
Removal of the HP Bleed Valve
AMM 36-11-51-400-802
Installation of the HP Bleed Valve
AMM 36-11-51-720-804
Functional Test of the HP Bleed Valve with the Test Set P/N 98D36109001000
3. Fault Confirmation
Subtask 36-11-00-710-434-A ** ON A/C NOT FOR ALL
A. Test
   (1) Not applicable.
4. Fault Isolation
Subtask 36-11-00-810-331-A ** ON A/C NOT FOR ALL
A. If the fault symptom is identified by the maintenance message HP BLEED-V (4000HA1):
   (1) Turn the manual shaft of the HP Bleed valve to OPEN.
   (2) Let the manual shaft go back to closed postion.
     (a) If the valve does not go back to the closed position:
     (b) If the valve go back to the closed position:
       1 If the test is not OK:
       2 If the test is OK:
  • Continue the trouble shooting procedure.
Subtask 36-11-00-710-665-A ** ON A/C NOT FOR ALL
B. If the fault symptom is identified by maintenance message AIR ENG 1 HP VALVE FAULT and there were large bleed pressure changes during flight phase 2 (ground idle) and/or flight phase 6 (top of descent):
   (1) Make sure that the IPCV is in the correct condition and not blocked in the open position AMM 36-11-41-200-802.
     (a) If the IPCV is damaged:
     (b) If the IPCV is in the correct condition:
  • Continue the trouble shooting procedure.
Subtask 36-11-00-810-333-A ** ON A/C NOT FOR ALL
C. If the fault continues:
   (1) Do a check of the wiring from the High Pressure Valve (4000HA1) pin A/1 and A/2 to BMC1 (1HA1) pin AB/14D and AB/12D ASM 361101.
   (2) If the wiring is damaged:
     (a) Repair or replace the wiring .
Subtask 36-11-00-810-370-A ** ON A/C NOT FOR ALL
D. If the fault continues:
   (1) Do a check of the wiring from the High Pressure Valve (4000HA1) pin A/1 and A/2 to BMC2 (1HA2) pin AB/15D AB/13D ASM 361101.
   (2) If the wiring is damaged:
     (a) Repair or replace the wiring .
Subtask 36-11-00-710-435-A ** ON A/C NOT FOR ALL
E. Test
   (1) After the subsequent flight, make sure that the fault does not continue.
[Rev.8 from Aug 2018] 2026.04.04 04:33:52 UTC