W DOC AIRBUS | TSM A320F

Loss of Bleed Air from the Engine 1 because of Starter-Valve Opening Indication


TASK 36-11-00-810-959-A
Loss of Bleed Air from the Engine 1 because of Starter-Valve Opening Indication


1. Possible Causes
  • BMC-1 [1HA1]
  • wiring
  • P/BSW-ENG 1 BLEED [4HA1]
  • ENG/APU FIRE PNL [1WD]
  • SOLENOID-BLEED PRESS REG V CTL, ENG 1 [10HA1]
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
TSM TASK 80-11-00-810-801-A
Failure of the Starter Shutoff Valve Switch on Engine 1
AMM 26-12-12-000-001
Removal of the ENG/APU Fire Panel
AMM 26-12-12-400-001
Installation of the ENG/APU Fire Panel
ASM 361101
AMM 36-11-34-000-001
Removal of the BMC
AMM 36-11-34-400-001
Installation of the BMC
AMM 36-11-55-000-001
Removal of the Bleed-Pressure-Regulator Valve Control-Solenoid
AMM 36-11-55-400-001
Installation of the Bleed-Pressure-Regulator Valve Control-Solenoid
3. Fault Confirmation
Subtask 36-11-00-710-406-A ** ON A/C NOT FOR ALL
A. Test
   (1) Not applicable, the fault is evident.
4. Fault Isolation
Subtask 36-11-00-810-253-A ** ON A/C NOT FOR ALL
A. If fault message SAV (SW) J9/J10 ECU is found then:
   (1) If the fault continues:
     (a) If the fault continues:
  • Do a check of the wiring ASM 361101 between:
    . Pin 2 of the AIR BLEED/ENG 1/CTL circuit breaker (3HA1) and pin AA/8A of the BMC 1 (1HA1)
    . Pin 2 of the AIR BLEED/ENG 1/CTL circuit breaker and pin A/D2 of the ENG 1 BLEED pushbutton switch (4HA1)
    . Pin AA/7A of the BMC 1 and pin A/D1 of the ENG 1 BLEED pushbutton switch
    . Pin A/D3 of the ENG 1 BLEED pushbutton switch and pin A/1 of the bleed pressure regulator valve control solenoid (10HA1)
    . Pin A/2 of the engine 1 bleed pressure regulator valve control solenoid and the ground.
       1 If the wiring is not correct:
  • Repair the wiring.
       2 If the wiring is correct:
  • Replace the P/BSW-ENG 1 BLEED [4HA1] .
         a If the fault continues:
Subtask 36-11-00-810-253-B ** ON A/C NOT FOR ALL
A. If failure message SAV (SW) J9/10 ECU is found then:
   (1) If the fault continues:
     (a) If the fault continues:
  • Do a check of the wiring ASM 361101 between:
    . Pin 2 of the AIR BLEED/ENG 1/CTL circuit breaker (3HA1) and pin AA/8A of the BMC 1 (1HA1)
    . Pin 2 of the AIR BLEED/ENG 1/CTL circuit breaker and pin A/D2 of the ENG 1 BLEED pushbutton switch (4HA1)
    . Pin AA/7A of the BMC 1 and pin A/D1 of the ENG 1 BLEED pushbutton switch
    . Pin A/D3 of the ENG 1 BLEED pushbutton switch and pin A/1 of the bleed pressure regulator valve control solenoid (10HA1)
    . Pin A/2 of the engine 1 bleed pressure regulator valve control solenoid and the ground.
       1 If the wiring is not correct:
  • Repair the wiring.
       2 If the wiring is correct:
  • Replace the P/BSW-ENG 1 BLEED [4HA1] .
         a If the fault continues:
Subtask 36-11-00-710-407-A ** ON A/C NOT FOR ALL
B. After the subsequent flight, make sure that the fault does not continue.
[Rev.8 from Aug 2018] 2026.04.04 04:33:51 UTC