W DOC AIRBUS | TSM A320F

Failure of the Overpressure Valve in Closed Position on the Engine 2


TASK 36-11-00-810-946-A
Failure of the Overpressure Valve in Closed Position on the Engine 2


1. Possible Causes
  • VALVE-OVERPRESSURE, ENG 2 [5HA2]
  • wiring
  • VALVE-HP BLEED [4000HA]
  • sense line
  • sense line between the bleed pressure-regulator valve (4001HA) and the HP bleed valve (4000HA)
  • VALVE-BLEED PRESS REG [4001HA]
  • sense line between the bleed pressure regulator valve (4001HA) and the HP bleed valve (4000HA)
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
ASM 361102
AMM 36-11-49-000-029
Removal of the Pneumatic Sense Lines in the Pylon
AMM 36-11-49-000-042
Removal of the Pylon Interface Duct
AMM 36-11-49-400-029
Installation of the Pneumatic Sense Lines in the Pylon
AMM 36-11-49-400-042
Installation of the Pylon Interface Duct
AMM 36-11-51-000-040
Removal of the High Pressure Bleed Valve
AMM 36-11-51-000-042
Removal of the High Pressure Bleed Valve
AMM 36-11-51-400-040
Installation of the High Pressure Bleed Valve
AMM 36-11-51-400-042
Installation of the High Pressure Bleed Valve
AMM 36-11-52-000-040
Removal of the Bleed Pressure-Regulator Valve
AMM 36-11-52-000-042
Removal of the Bleed Pressure Regulator Valve
AMM 36-11-52-400-040
Installation of the Bleed Pressure-Regulator Valve
AMM 36-11-52-400-042
Installation of the Bleed Pressure Regulator Valve
AMM 36-11-53-000-001
Removal of the Overpressure Valve
AMM 36-11-53-400-001
Installation of the Overpressure Valve
AMM 36-11-53-720-001
Functional Test of the Overpressure Valves with the Bleed Test Set P/N 98D36003000000
3. Fault Confirmation
Subtask 36-11-00-720-053-A ** ON A/C NOT FOR ALL
A. Test
   (1) Do the functional test of the engine 2 overpressure valve (5HA2) AMM 36-11-53-720-001.
4. Fault Isolation
Subtask 36-11-00-810-240-A ** ON A/C NOT FOR ALL
A. If the functional test of the engine 2 overpressure valve (5HA2) is not correct:
   (1) If the fault continues:
  • do a check and repair the wiring between:
    . pin A/1 of the engine 2 overpressure valve (5HA2) and pin AA/10A of the BMC2 (1HA2)
    . pin A/2 of the engine 2 overpressure valve and the ground ASM 361102.
Subtask 36-11-00-810-242-A ** ON A/C NOT FOR ALL
B. If the functional test of the engine 2 overpressure valve (5HA2) is correct:
   (1) If the fault continues:
  • do a leak check on the sense line between the bleed pressure regulator valve (4001HA) and the HP bleed valve (4000HA).
     (a) If there is a leak:
     (b) If there is no leak:
Subtask 36-11-00-810-242-C ** ON A/C NOT FOR ALL
B. If the functional test of the engine 2 overpressure valve (5HA2) is correct:
   (1) If the fault continues:
  • do a leak check on the sense line between the bleed pressure regulator valve (4001HA) and the HP bleed valve (4000HA).
     (a) If there is a leak:
     (b) If there is no leak:
Subtask 36-11-00-720-054-A ** ON A/C NOT FOR ALL
C. After the subsequent flight, make sure that the fault does not continue.
[Rev.8 from Aug 2018] 2026.04.04 04:33:50 UTC