High Bleed Temperature of the Engine 2 in Cruise
TASK 36-11-00-810-891-A
High Bleed Temperature of the Engine 2 in Cruise
1. Possible Causes
2. Job Set-up Information
A. Referenced Information
3. Fault Confirmation
Subtask 36-11-00-710-229-A ** ON A/C NOT FOR ALL 4. Fault Isolation
Subtask 36-11-00-810-141-A ** ON A/C NOT FOR ALL
[Rev.8 from Aug 2018]
2026.04.04 04:33:48 UTC
High Bleed Temperature of the Engine 2 in Cruise
1. Possible Causes
2. Job Set-up Information
A. Referenced Information
| REFERENCE | DESIGNATION |
|---|---|
| AMM 36-11-00-740-001 | BITE Test of the BMC 1(2) |
| AMM 36-11-51-000-040 | Removal of the High Pressure Bleed Valve |
| AMM 36-11-51-000-042 | Removal of the High Pressure Bleed Valve |
| AMM 36-11-51-400-040 | Installation of the High Pressure Bleed Valve |
| AMM 36-11-51-400-042 | Installation of the High Pressure Bleed Valve |
| AMM 36-11-54-000-001 | Removal of the Fan Air Valve |
| AMM 36-11-54-400-001 | Installation of the Fan Air Valve |
Subtask 36-11-00-710-229-A ** ON A/C NOT FOR ALL 4. Fault Isolation
Subtask 36-11-00-810-141-A ** ON A/C NOT FOR ALL
A. If the test gives a maintenance message:
Subtask 36-11-00-810-141-C ** ON A/C NOT FOR ALL - Do the trouble shooting procedure related to the maintenance message.
- replace the VALVE-FAN AIR, ENG2 [9HA2] AMM 36-11-54-000-001 and AMM 36-11-54-400-001.
- replace the VALVE-HP BLEED [4000HA] AMM 36-11-51-000-040 and AMM 36-11-51-400-040.
A. If the test gives a maintenance message:
Subtask 36-11-00-710-230-A ** ON A/C NOT FOR ALL - Do the trouble shooting procedure related to the maintenance message.
- replace the VALVE-FAN AIR, ENG2 [9HA2] AMM 36-11-54-000-001 and AMM 36-11-54-400-001.
- replace the VALVE-HP BLEED [4000HA] AMM 36-11-51-000-042 and AMM 36-11-51-400-042.
B. After the subsequent flight, make sure that the fault does not continue.