W DOC AIRBUS | TSM A320F

High Bleed Temperature of the Engine 1 in Cruise


TASK 36-11-00-810-884-A
High Bleed Temperature of the Engine 1 in Cruise


1. Possible Causes
  • VALVE-FAN AIR, ENG1 [9HA1]
  • VALVE-HP BLEED [4000HA]
2. Job Set-up Information
 A. Referenced Information
REFERENCE
DESIGNATION
AMM 36-11-00-740-001
BITE Test of the BMC 1(2)
AMM 36-11-51-000-040
Removal of the High Pressure Bleed Valve
AMM 36-11-51-000-042
Removal of the High Pressure Bleed Valve
AMM 36-11-51-400-040
Installation of the High Pressure Bleed Valve
AMM 36-11-51-400-042
Installation of the High Pressure Bleed Valve
AMM 36-11-54-000-001
Removal of the Fan Air Valve
AMM 36-11-54-400-001
Installation of the Fan Air Valve
3. Fault Confirmation
Subtask 36-11-00-710-215-A ** ON A/C NOT FOR ALL
A. Test
   (1) Do the BITE test of the BMC1 AMM 36-11-00-740-001.
4. Fault Isolation
Subtask 36-11-00-810-134-A ** ON A/C NOT FOR ALL
A. If the test gives a maintenance message:
  • Do the trouble shooting procedure related to the maintenance message.
   (1) If there is no maintenance message:
     (a) If the fault continues:
Subtask 36-11-00-810-134-C ** ON A/C NOT FOR ALL
A. If the test gives a maintenance message:
  • Do the trouble shooting procedure related to the maintenance message.
   (1) If there is no maintenance message:
     (a) If the fault continues:
Subtask 36-11-00-710-216-A ** ON A/C NOT FOR ALL
B. After the subsequent flight, make sure that the fault does not continue.
[Rev.8 from Aug 2018] 2026.04.04 04:33:47 UTC