Downstream NAI Valve Failed Open with NAI Pushbutton Switch Released on Channels A and B
TASK 30-21-00-810-821-A
Downstream NAI Valve Failed Open with NAI Pushbutton Switch Released on Channels A and B
1. Possible Causes
A. Fixtures, Tools, Test and Support Equipment
B. Referenced Information
3. Fault Confirmation
Subtask 30-21-00-730-058-A ** ON A/C NOT FOR ALL
Subtask 30-21-00-942-062-A ** ON A/C NOT FOR ALL
[Rev.8 from Aug 2018]
2026.04.04 04:29:32 UTC
Downstream NAI Valve Failed Open with NAI Pushbutton Switch Released on Channels A and B
1. Possible Causes
- NAI SOLENOID BLOCK [4190KS]
- NACELLE ANTI-ICE LOWER VALVE AND ATTACHMENT HARDWARE [4011DN]
- W04 HARNESS [4088KS]
- W03 HARNESS [4087KS]
- PRESS XDCR-ENGINE AIR INTAKE ANTI ICE, 2 [4003DN]
[4000KS]
A. Fixtures, Tools, Test and Support Equipment
| REFERENCE | QTY | DESIGNATION |
|---|---|---|
| No specific | 1 | PLIERS - JAWED, SOFT |
| REFERENCE | DESIGNATION |
|---|---|
| TSM TASK 71-00-00-810-835-A | Component and Harness Intermittent Troubleshooting Procedure for Guidance Troubleshooting Intermittent Faults |
| AMM 30-21-00-710-002 | Operational Test of the Engine Air Intake Ice Protection (with the Engines in operation) |
| AMM 30-21-21-000-801 | Removal of the Nacelle Anti-Ice Solenoid-Manifold |
| AMM 30-21-21-400-801 | Installation of the Nacelle Anti-Ice Solenoid-Manifold |
| AMM 30-21-23-000-801 | Removal of the Nacelle Anti-Ice Fan-Pressure-Transducer |
| AMM 30-21-23-400-801 | Installation of the Nacelle Anti-Ice Fan-Pressure-Transducer |
| AMM 30-21-51-000-803 | Removal of the Lower Anti-Ice Valve |
| AMM 30-21-51-400-803 | Installation of the Lower Anti-Ice Valve |
| AMM 31-32-00-860-012 | Procedure to Get Access to the SYSTEM REPORT/TEST/ENG Page |
| AWM 715134 | |
| AMM 73-21-01-000-801 | Removal of the Electronic Engine Control (EEC) |
| AMM 73-21-01-400-801 | Installation of the Electronic Engine Control (EEC) |
| AMM 73-21-63-000-802 | Removal of the Electronic Engine Control (EEC) Wiring Harness (W03) |
| AMM 73-21-63-400-802 | Installation of the Electronic Engine Control (EEC) Wiring Harness (W03) |
| AMM 73-21-64-000-802 | Removal of the Electronic Engine Control (EEC) Wiring Harness (W04) |
| AMM 73-21-64-400-802 | Installation of the Electronic Engine Control (EEC) Wiring Harness (W04) |
| AMM 78-36-00-010-802 | Opening of the Thrust Reverser Cowl-Doors |
| AMM 78-36-00-410-802 | Closing of the Thrust Reverser Cowl-Doors |
Subtask 30-21-00-730-058-A ** ON A/C NOT FOR ALL
A. Test
(1) Do the operational test of the engine air-intake ice-protection AMM 30-21-00-710-002.
(2) On the MCDU screen, get access to the SYSTEM REPORT/TEST/ENG menu page AMM 31-32-00-860-012.
(a) On the SYSTEM REPORT/TEST/ENG menu page, push the line key adjacent to the FADEC 1(2) A(B) indication.
The EEC 1(2) CHAN A(B) page comes into view.
(b) Push the line key adjacent to the GND SCANNING indication, the GROUND SCANNING menu page comes into view.
1 If there is a maintenance message, go to the Para. Fault Isolation.
2 If the maintenance message does not come into view again, do the component and harness intermittent for guidance troubleshooting intermittent faults (Ref. TSM TASK 71-00-00-810-835).
a If you find no fault, send the engine back to service. Monitor the engine to make sure that the maintenance message does not come into view again.
4. Fault Isolation(1) Do the operational test of the engine air-intake ice-protection AMM 30-21-00-710-002.
(2) On the MCDU screen, get access to the SYSTEM REPORT/TEST/ENG menu page AMM 31-32-00-860-012.
(a) On the SYSTEM REPORT/TEST/ENG menu page, push the line key adjacent to the FADEC 1(2) A(B) indication.
The EEC 1(2) CHAN A(B) page comes into view.
(b) Push the line key adjacent to the GND SCANNING indication, the GROUND SCANNING menu page comes into view.
1 If there is a maintenance message, go to the Para. Fault Isolation.
2 If the maintenance message does not come into view again, do the component and harness intermittent for guidance troubleshooting intermittent faults (Ref. TSM TASK 71-00-00-810-835).
a If you find no fault, send the engine back to service. Monitor the engine to make sure that the maintenance message does not come into view again.
WARNING:
BE CAREFUL WHEN YOU DO WORK ON THE ENGINE AFTER SHUTDOWN. THE ENGINE CAN STAY HOT FOR A LONG TIME. IF YOU DO NOT OBEY THIS WARNING, INJURY CAN OCCUR.
CAUTION:
MAKE SURE YOU REMOVE ELECTRICAL POWER FROM THE EEC BEFORE YOU REMOVE THE ELECTRICAL CONNECTORS. IF YOU DO NOT OBEY THIS INSTRUCTION, DAMAGE TO THE EEC CAN OCCUR.
Subtask 30-21-00-810-070-A ** ON A/C NOT FOR ALL A. If there is confirmation of the fault:
(1) Open the right thrust-reverser cowl-door AMM 78-36-00-010-802.
Use PLIERS - JAWED, SOFT to disconnect electrical connector P14 of the EEC.
5. Close-up(1) Open the right thrust-reverser cowl-door AMM 78-36-00-010-802.
- Replace the NAI SOLENOID BLOCK [4190KS] , AMM 30-21-21-000-801 and AMM 30-21-21-400-801 and replace the NACELLE ANTI-ICE LOWER VALVE AND ATTACHMENT HARDWARE [4011DN] , AMM 30-21-51-000-803 and AMM 30-21-51-400-803.
- Do the test given in Para. 3.
- Use PLIERS - JAWED, SOFT to disconnect electrical connector P13 of the EEC.
- Examine electrical connector P13 of the EEC for bent pins, contamination or corrosion or signs of damage.
- Replace the W04 HARNESS [4088KS] AMM 73-21-63-000-802 and AMM 73-21-63-400-802.
- Do the test given in Para. 3.
- Do a continuity check of the W04 harness AWM 715134 between:
. Pin P13/q of the EEC and pin P17/12 of the NAI fan pressure-transducer (4003DN)
. Pin P13/BB of the EEC and pin P17/4 of the NAI fan pressure-transducer (4003DN)
. Pin P13/p of the EEC and pin P17/3 of the NAI fan pressure-transducer (4003DN)
. Pin P13/T of the EEC and pin P17/11 of the NAI fan pressure-transducer. (4003DN).
- Replace the W04 HARNESS [4088KS] AMM 73-21-64-000-802 and AMM 73-21-64-400-802.
- Do the test given in Para. 3.
Use PLIERS - JAWED, SOFT to disconnect electrical connector P14 of the EEC.
- Examine electrical connector P14 of the EEC for bent pins, contamination or corrosion or signs of damage.
- Replace the W03 HARNESS [4087KS] AMM 73-21-63-000-802 and AMM 73-21-63-400-802.
- Do the test given in Para. 3.
- Do a continuity check of the W03 harness AWM 715134 between:
. Pin P14/q of the EEC and P106/11 of 4100VC
. Pin P14/BB of the EEC and P106/12 of 4100VC
. Pin P14/p of the EEC and P106/25 of 4100VC
. Pin P14/T of the EEC and P106/26 of 4100VC. - If there is no continuity:
- Replace the W03 HARNESS [4087KS] AMM 73-21-63-000-802 and AMM 73-21-63-400-802.
- Do the test given in Para. 3.
- If there is continuity:
- Do a continuity check of the W04 harness AWM 715134 between:
. Pin P17/9 of the NAI fan pressure-transducer (4003DN) and J106/11 of 4100VC
. Pin P17/8 of the NAI fan pressure-transducer (4003DN) and J106/12 of 4100VC
. Pin P17/7 of the NAI fan pressure-transducer (4003DN) and J106/25 of 4100VC
. Pin P17/6 of the NAI fan pressure-transducer (4003DN) and J106/26 of 4100VC. - If there is no continuity:
- Replace the W04 HARNESS [4088KS] AMM 73-21-64-000-802 and AMM 73-21-64-400-802.
- Do the test given in Para. 3.
- Replace PRESS XDCR-ENGINE AIR INTAKE ANTI ICE, 2 [4003DN] AMM 30-21-23-000-801 and AMM 30-21-23-400-801.
- Do the test given in Para. 3.
- Replace the
[4000KS] AMM 73-21-01-000-801 and AMM 73-21-01-400-801. - Do the test given in Para. 3.
Subtask 30-21-00-942-062-A ** ON A/C NOT FOR ALL
A. Put the aircraft back to its initial configuration.
(1) Make sure that the work area is clean and clear of tools and other items.
(a) Close the right thrust-reverser cowl-door AMM 78-36-00-410-802.
(1) Make sure that the work area is clean and clear of tools and other items.
(a) Close the right thrust-reverser cowl-door AMM 78-36-00-410-802.