Intercell XFR Valve 28QM/71QM/11QP (Left Rear) Fault - Stays Closed When The Fuel In The Inner-cell Is At Low Level
TASK 28-15-00-810-804-A
Intercell XFR Valve 28QM/71QM/11QP (Left Rear) Fault - Stays Closed When The Fuel In The Inner-cell Is At Low Level
A. Fixtures, Tools, Test and Support Equipment
B. Referenced Information
3. Fault Confirmation
Subtask 28-15-00-865-056-A ** ON A/C NOT FOR ALL
Subtask 28-15-00-810-053-A ** ON A/C NOT FOR ALL
[Rev.8 from Aug 2018]
2026.04.04 04:39:26 UTC
Intercell XFR Valve 28QM/71QM/11QP (Left Rear) Fault - Stays Closed When The Fuel In The Inner-cell Is At Low Level
WARNING:
OBEY THE FUEL SAFETY PROCEDURES.
WARNING:
WHEN YOU DO WORK ON THE FUEL SYSTEM WIRING, YOU MUST USE TEST EQUIPMENT THAT IS APPROVED (REFER TO INTERNATIONAL OR NATIONAL SPECIFICATIONS FOR INTRINSICALLY SAFE TEST EQUIPMENT: EN50020, UL913 OR EQUIVALENT). TEST EQUIPMENT THAT IS NOT APPROVED CAN CAUSE FIRE OR AN EXPLOSION.
1. Possible Causes- ACTUATOR-TRANSFER VALVE, L REAR SPAR [11QP]
- aircraft wiring
RELAY-L WING TK LOW LEVEL CHANNEL A (5QP) RELAY-R WING TK LOW LEVEL CHANNEL B (6QP) RELAY-L OR R REAR XFR VALVE OPEN LATCH (13QP)
A. Fixtures, Tools, Test and Support Equipment
| REFERENCE | QTY | DESIGNATION |
|---|---|---|
| No specific | AR | MULTIMETER - STANDARD |
| REFERENCE | DESIGNATION |
|---|---|
| ESPM 2053210 | |
| AMM 28-15-00-740-002 | Functional (BITE) Test of the Intercell Transfer Valves |
| ASM 281501 | |
| AMM 28-15-51-000-002 | Removal of the Actuator |
| AMM 28-15-51-400-002 | Installation of the Actuator |
| AMM 28-46-00-740-001 | Functional (BITE) Test |
Subtask 28-15-00-865-056-A ** ON A/C NOT FOR ALL
A. Table of the circuit breakers used in this procedure:
Subtask 28-15-00-710-053-A ** ON A/C NOT FOR ALL | PANEL | DESIGNATION | FIN | LOCATION |
|---|---|---|---|
| ** ON A/C NOT FOR ALL | |||
| 49VU | FUEL/FQI/CHAN/1 | 1QT | A13 |
| 49VU | FUEL/XFR VALVE1/WING/R | 2QP | A11 |
| 49VU | FUEL/XFR VALVE1/WING/L | 1QP | A10 |
| 121VU | FUEL/FQI/CHAN/2 | 2QT | M27 |
B. Test
(1) Do the Functional BITE Test (of the FLSS) AMM 28-46-00-740-001.
(a) Examine the FLSS STATUS page.
Look for one (or more) of the messages that follow:
Look for the (left wing rear ICTV) message XFR VALVE 28QM/71QM/11QP.
(b) If the message:
4. Fault Isolation(1) Do the Functional BITE Test (of the FLSS) AMM 28-46-00-740-001.
(a) Examine the FLSS STATUS page.
Look for one (or more) of the messages that follow:
- L LO LEVEL SENSOR 16QJ1
- R LO LEVEL SENSOR 15QJ2
- FLSCU1 7QJ
- FLSCU2 9QJ.
- is not shown, do step (2)
- is shown, trouble shoot the LRU(s) before you do step (2). Refer to the Fault Symptoms List/28-CFDS for the related Task number.
NOTE: The COMMAND FLSS BITE option does not test the Intercell Transfer Valves (ICTVs).
NOTE: The ICTVs are motor driven and the electrical power for these circuits is supplied from 801PP, 28VDC, ESS BUS/SHEDDABLE ASM 281501. The ICTVs will not operate on battery power.
(a) Examine the FLSS STATUS page. Look for the (left wing rear ICTV) message XFR VALVE 28QM/71QM/11QP.
(b) If the message:
- is shown, do Para. 4.A.
- is not shown, no work steps are necessary.
Subtask 28-15-00-810-053-A ** ON A/C NOT FOR ALL
A. Procedure
(1) Make sure that the C/B 1QP is closed.
(2) Open the C/B 2QP.
(3) Get access to the ACTUATOR-TRANSFER VALVE, L REAR SPAR (11QP) AMM 28-15-51-000-002.
(4) Disconnect the electrical connector 11QP-A from the ACTUATOR-TRANSFER VALVE, L REAR SPAR (11QP).
(5) Do a test, with a MULTIMETER - STANDARD, to see if 28VDC is available at pin A of the connector 11QP-A ASM 281501.
(a) If the 28VDC:
(a) When the actuator is removed from the aircraft make sure that the transfer valve drive shaft and valve are free to rotate.
(b) Repair/replace all the unserviceable items found in (a).
(c) Do the test given in Para. 3.B.(2).
(7) Close the C/B 2QP.
(8) Do a test, with a multimeter, to make sure that 28VDC is available at the RELAY-L WING TK LOW LEVEL CHANNEL A (5QP) terminals A2 and X1 ASM 281501.
(a) If the 28VDC:
(a) Repair all the unserviceable wiring and connectors ESPM 2053210.
(b) Do the test given in Para.3.B.(2).
(10) Do a test, with a multimeter, to make sure that 28VDC is available at the RELAY-R WING TK LOW LEVEL CHANNEL B (6QP) terminals A2 and X1 ASM 281501.
(a) If the 28VDC:
(a) Repair all the unserviceable wiring and connectors ESPM 2053210.
(b) Do the test given in Para. 3.B.(2).
(12) If the fault continues:
(a) Do a check of and replace, if necessary, the relays that follow:
(13) If the fault continues:
(a) Do a wiring check of the aircraft wiring ASM 281501 between:
(15) Do the test given in Para. 3.B.(2).
(1) Make sure that the C/B 1QP is closed.
(2) Open the C/B 2QP.
(3) Get access to the ACTUATOR-TRANSFER VALVE, L REAR SPAR (11QP) AMM 28-15-51-000-002.
(4) Disconnect the electrical connector 11QP-A from the ACTUATOR-TRANSFER VALVE, L REAR SPAR (11QP).
(5) Do a test, with a MULTIMETER - STANDARD, to see if 28VDC is available at pin A of the connector 11QP-A ASM 281501.
(a) If the 28VDC:
- is available, do step (6)
- is not available, continue at step (7).
(a) When the actuator is removed from the aircraft make sure that the transfer valve drive shaft and valve are free to rotate.
(b) Repair/replace all the unserviceable items found in (a).
(c) Do the test given in Para. 3.B.(2).
(7) Close the C/B 2QP.
(8) Do a test, with a multimeter, to make sure that 28VDC is available at the RELAY-L WING TK LOW LEVEL CHANNEL A (5QP) terminals A2 and X1 ASM 281501.
(a) If the 28VDC:
- is not available, do step (9)
- is available, continue at step (10).
(a) Repair all the unserviceable wiring and connectors ESPM 2053210.
(b) Do the test given in Para.3.B.(2).
(10) Do a test, with a multimeter, to make sure that 28VDC is available at the RELAY-R WING TK LOW LEVEL CHANNEL B (6QP) terminals A2 and X1 ASM 281501.
(a) If the 28VDC:
- is not available, do step (11)
- is available, continue at step (12).
(a) Repair all the unserviceable wiring and connectors ESPM 2053210.
(b) Do the test given in Para. 3.B.(2).
(12) If the fault continues:
(a) Do a check of and replace, if necessary, the relays that follow:
RELAY-L WING TK LOW LEVEL CHANNEL A (5QP) RELAY-R WING TK LOW LEVEL CHANNEL B (6QP) RELAY-L OR R REAR XFR VALVE OPEN LATCH (13QP) .
(13) If the fault continues:
(a) Do a wiring check of the aircraft wiring ASM 281501 between:
- the ACTUATOR connector 11QP-A, pin A and the RELAY 5QP, terminal A3
- the ACTUATOR connector 11QP-A, pin A and the RELAY 6QP, terminal B3
- the RELAY 5QP, terminal A1 and the RELAY 6QP, terminal B2
- the RELAY 5QP, terminal X2 and the RELAY 13QP, terminal A
- the RELAY 6QP, terminal X2 and the RELAY 13QP, terminal B
- the RELAY 13QP, terminal 1 and the FLSCU-1 rack connector 7QJ-AA, pin 5A
- the RELAY 13QP, terminal 3 and the FLSCU-2 rack connector 9QJ-AA, pin 5A.
(15) Do the test given in Para. 3.B.(2).