LGCIU Signal Mismatch
TASK 26-22-00-810-805-A
LGCIU Signal Mismatch
1. Possible Causes
A. Referenced Information
3. Fault Confirmation
Subtask 26-22-00-710-054-A
Subtask 26-22-00-810-061-A
Subtask 26-22-00-860-054-A
[Rev.8 from Aug 2018]
2026.04.04 04:27:24 UTC
LGCIU Signal Mismatch
1. Possible Causes
RELAY-FLIGHT/GROUND (43WF) RELAY-AUTO TIME DELAY PUSH (39WF) - wiring
A. Referenced Information
| REFERENCE | DESIGNATION |
|---|---|
| AMM 26-22-00-710-001 | Operational Test of the APU Fire-Extinguishing Loop/Squib |
| ASM 262202 | |
| AMM 32-69-00-740-001 | BITE Check of Landing-Gear Control Interface-Unit (LGCIU) With Use of MCDU to Ensure that Continuous BITE is Operative |
Subtask 26-22-00-710-054-A
A. The APU FIRE EXTINGUISHING PANEL 20VU (p/n 330TS08Y) has a fault. Special operation is necessary. Incorrect operation causes the APU fire extinguisher bottle to discharge. Airbus supplies a new 20VU panel that corrects this fault. See TFU 26.22.00.007 for more data.
(1) Maintenance recommendation:
(a) Before the test:
4. Fault Isolation(1) Maintenance recommendation:
(a) Before the test:
- Pull the CIRCUIT BREAKER 30WF on panel 120VU.
- Push the APU FIRE TEST BUTTON quickly and fully.
- Hold it fully during the test.
- Release it quickly.
- Close the CIRCUIT BREAKER 30WF on panel 120VU.
Subtask 26-22-00-810-061-A
A. If the test gives a different maintenance message:
Subtask 26-22-00-810-060-A - Do the trouble shooting procedure related to the maintenance message.
B. If the test gives the maintenance message APU FIRE:
do a check of theRELAY-AUTO TIME DELAY PUSH (39WF) and replace it if necessary ASM 262202.
(2) If the fault continues:
Subtask 26-22-00-710-059-A - do a check of the
RELAY-FLIGHT/GROUND (43WF) and replace it if necessary ASM 262202.
do a check of the
(2) If the fault continues:
- do the BITE test of the landing gear AMM 32-69-00-740-001.
- Do the trouble shooting procedure related to the maintenance message.
- do a check and repair the wiring if necessary between:
RELAY (43WF) connector A/X1 and LGCIU 1 (5GA1) connector AA/5B,
RELAY (43WF) connector A/A2 and RELAY (39WF) connector A/A2,
RELAY (39WF) connector A/A1 and BODY-LIGHT (40WF),
RELAY (43WF) connector A/A1 and CB (30WF),
RELAY (43WF) connector A/X2 and GND ASM 262202.
C. Do the test as given in the Para. 3.A.
5. Close-upSubtask 26-22-00-860-054-A
A. Put the aircraft back to its initial configuration.