Loss of the 601PP and 602PP busbars in Normal Configuration
TASK 24-61-00-810-801-A
Loss of the 601PP and 602PP busbars in Normal Configuration
1. Possible Causes
A. Referenced Information
3. Fault Confirmation
Subtask 24-61-00-860-050-A Subtask 24-61-00-710-050-A
Subtask 24-61-00-865-050-A
Subtask 24-61-00-860-051-A
[Rev.8 from Aug 2018]
2026.04.04 04:26:59 UTC
Loss of the 601PP and 602PP busbars in Normal Configuration
1. Possible Causes
- wiring
- C/B-DC SVCE/602PP/SPLY [7PN]
- CNTOR-DC SVCE BUS NORM SPLY [8PN]
- CNTOR-DC SVCE BUS GND SPLY [3PX]
- C/B-ELEC/DC/SVCE/BUS [5PN]
A. Referenced Information
| REFERENCE | DESIGNATION |
|---|---|
| TSM TASK 24-00-00-810-803-A | Circuit Breaker Tripped and/or C/B TRIPPED Warning |
| AMM 24-41-00-861-002 | Energize the Aircraft Electrical Circuits from the External Power |
| AMM 24-41-00-862-002 | De-energize the Aircraft Electrical Circuits Supplied from the External Power |
| ASM 244301 | |
| AMM 24-43-55-000-001 | Removal of the DC Service Bus Ground Supply Contactor |
| AMM 24-43-55-400-001 | Installation of the DC Service Bus Ground Supply Contactor |
| ASM 246101 | |
| AMM 24-61-55-000-001 | Removal of the DC Service Bus Normal Supply Contactor |
| AMM 24-61-55-400-001 | Installation of the DC Service Bus Normal Supply Contactor |
Subtask 24-61-00-860-050-A Subtask 24-61-00-710-050-A
B. Test
4. Fault Isolation| ACTION | RESULT |
|---|---|
1.On the overhead panel 25VU:
|
|
Subtask 24-61-00-865-050-A
A. Table of the circuit breakers used in this procedure:
Subtask 24-61-00-810-050-A | PANEL | DESIGNATION | FIN | LOCATION |
|---|---|---|---|
| ** ON A/C ALL | |||
| 122VU | ELEC/DC/SVCE/BUS | 5PN | X24 |
| 124VU | DC SVCE/602PP/SPLY | 7PN | BD01 |
B. If the test confirms the fault:
Subtask 24-61-00-710-051-A - Do a check of the status of the circuit breaker (7PN).
- Do a check for 28VDC on the pin F of the contactor (8PN) ASM 246101.
- Do a check of the wiring between the circuit breaker (7PN) and the contactor (8PN) ASM 246101.
- Repair the wiring.
- Replace the C/B-DC SVCE/602PP/SPLY [7PN] .
- Do a check for 28VDC on the pin 3 of the contactor (8PN) ASM 246101.
- Replace the CNTOR-DC SVCE BUS NORM SPLY [8PN] AMM 24-61-55-000-001 and AMM 24-61-55-400-001.
- Do a check and repair the wiring between A/E of the contactor (8PN) and the busbars 601PP and 602PP ASM 244301.
- Do a check of the wiring between the circuit breaker (5PN) and the pin 3 of the contactor (8PN) ASM 246101.
- Repair the wiring.
- Replace the CNTOR-DC SVCE BUS GND SPLY [3PX] AMM 24-43-55-000-001 and AMM 24-43-55-400-001.
- Replace the C/B-ELEC/DC/SVCE/BUS [5PN] .
- Do the procedure (Ref. TSM TASK 24-00-00-810-803).
- Replace the C/B-DC SVCE/602PP/SPLY [7PN] .
C. Do the test given in Para. 3 and make sure that the CAPT dome lights come on.
5. Close-upSubtask 24-61-00-860-051-A
A. Put the aircraft back to its initial configuration.
(1) On the overhead panel 25VU, put the INT LT/DOME switch in the OFF position.
(2) De-energize the aircraft electrical circuits
AMM 24-41-00-862-002.
(1) On the overhead panel 25VU, put the INT LT/DOME switch in the OFF position.
(2) De-energize the aircraft electrical circuits
AMM 24-41-00-862-002.