Loss of the DC Essential Busbar with TR1 and TR2 in Operation
TASK 24-35-00-810-806-A
Loss of the DC Essential Busbar with TR1 and TR2 in Operation
1. Possible Causes
2. Job Set-up Information
A. Referenced Information
3. Fault Confirmation
Subtask 24-35-00-860-054-A
Subtask 24-35-00-810-069-A ** ON A/C NOT FOR ALL
Subtask 24-35-00-860-055-A
[Rev.8 from Aug 2018]
2026.04.04 04:26:46 UTC
Loss of the DC Essential Busbar with TR1 and TR2 in Operation
1. Possible Causes
2. Job Set-up Information
A. Referenced Information
| REFERENCE | DESIGNATION |
|---|---|
| AMM 24-35-00-960-801 | Replacement of the Fuse 20PC1 |
| AMM 24-41-00-861-002 | Energize the Aircraft Electrical Circuits from the External Power |
| AMM 24-41-00-862-002 | De-energize the Aircraft Electrical Circuits Supplied from the External Power |
| AMM 24-61-58-000-001 | Removal of the DC Bus 1 Contactor Module |
| AMM 24-61-58-400-001 | Installation of the DC Bus 1 Contactor Module |
| ASM 246201 | |
| AMM 31-60-00-860-001 | EIS Start Procedure |
| AMM 31-60-00-860-002 | EIS Stop Procedure |
Subtask 24-35-00-860-054-A
A. Aircraft Maintenance Configuration
(1) Energize the aircraft electrical circuits
AMM 24-41-00-861-002.
(2) On the ELEC panel 35VU, push the BAT1 and BAT2 pushbutton switches:
AMM 31-60-00-860-001.
Subtask 24-35-00-710-065-A (1) Energize the aircraft electrical circuits
AMM 24-41-00-861-002.
(2) On the ELEC panel 35VU, push the BAT1 and BAT2 pushbutton switches:
- The OFF legend goes off.
AMM 31-60-00-860-001.
B. Test
(1) Do this test:
4. Fault Isolation(1) Do this test:
| ACTION | RESULT |
|---|---|
On the ECAM control panel:
| The ELEC page comes into view with: On the lower ECAM display unit (DU):
|
Subtask 24-35-00-810-069-A ** ON A/C NOT FOR ALL
A. If the Test Confirms the Fault:
(1) Do a check for short to ground of the wiring ASM 246201 at:
Subtask 24-35-00-810-069-B ** ON A/C NOT FOR ALL (1) Do a check for short to ground of the wiring ASM 246201 at:
- Pin A/G of DC ESS-BUS supply contactor (4PC)
- Pin A/E of DC ESS-BUS supply contactor (4PC)
- Pin A/G of DC SHED ESS-BUS (8PH).
- Repair it.
- Replace HOLDER-FUSE [20PC] AMM 24-35-00-960-801.
A. If the Test Confirms the Fault:
(1) Do a check for short to ground of the wiring ASM 246201 at:
Subtask 24-35-00-710-066-A (1) Do a check for short to ground of the wiring ASM 246201 at:
- Pin A/G of DC ESS-BUS supply contactor (4PC)
- Pin A/E of DC ESS-BUS supply contactor (4PC)
- Pin A/G of DC SHED ESS-BUS (8PH).
- Repair it.
- Replace
[20PC] AMM 24-35-00-960-801.
- Replace MODULE-DC BUS 1 CNTOR [13PN] AMM 24-61-58-000-001 and AMM 24-61-58-400-001.
B. Do this Test to Make Sure that the System Operates Correctly:
5. Close-up| ACTION | RESULT |
|---|---|
On the ECAM control panel:
| The ELEC page comes into view, make sure that: On the lower ECAM DU:
|
Subtask 24-35-00-860-055-A
A. Put the Aircraft Back to its Initial Configuration
(1) Do the EIS stop procedure
AMM 31-60-00-860-002.
(2) De-energize the aircraft electrical circuits
AMM 24-41-00-862-002.
(1) Do the EIS stop procedure
AMM 31-60-00-860-002.
(2) De-energize the aircraft electrical circuits
AMM 24-41-00-862-002.