GEN 2 Voltage, Frequency and Load Indication Lost or Incorrect
TASK 24-22-00-810-807-A
GEN 2 Voltage, Frequency and Load Indication Lost or Incorrect
1. Possible Causes
A. Referenced Information
3. Fault Confirmation
Subtask 24-22-00-860-054-A
Subtask 24-22-00-865-054-A
Subtask 24-22-00-860-055-A
[Rev.8 from Aug 2018]
2026.04.04 04:26:34 UTC
GEN 2 Voltage, Frequency and Load Indication Lost or Incorrect
1. Possible Causes
- EGIU-2 [22XU2]
- C/B-GEN2/EGIU2/115VAC [23XU2]
- wiring
- feeder
- GCU-2 [1XU2]
- IDG [4000XU]
- IDG-ENG 2 [4000XU2]
A. Referenced Information
| REFERENCE | DESIGNATION |
|---|---|
| TSM TASK 24-00-00-810-803-A | Circuit Breaker Tripped and/or C/B TRIPPED Warning |
| AMM 24-21-51-000-040 | Removal of the Integrated Drive Generator - IDG 1(2) |
| AMM 24-21-51-000-803 | Removal of the Integrated Drive Generator - IDG 1(2) |
| AMM 24-21-51-400-040 | Installation of the Integrated Drive Generator - IDG 1(2) |
| AMM 24-21-51-400-803 | Installation of the Integrated Drive Generator - IDG 1(2) |
| ASM 242201 | |
| ASM 242202 | |
| AMM 24-22-33-000-001 | Removal of the EGIU-1(2) |
| AMM 24-22-33-400-002 | Installation of the EGIU-1(2) |
| AMM 24-22-34-000-001 | Removal of the GCU-1(2) |
| AMM 24-22-34-400-001 | Installation of the GCU-1(2) |
| AMM 24-41-00-861-002 | Energize the Aircraft Electrical Circuits from the External Power |
| AMM 24-41-00-862-002 | De-energize the Aircraft Electrical Circuits Supplied from the External Power |
| ASM 315403 | |
| AMM 31-60-00-860-001 | EIS Start Procedure |
| AMM 31-60-00-860-002 | EIS Stop Procedure |
Subtask 24-22-00-860-054-A
A. Job Set-up
(1) Aircraft Maintenance Configuration
(a) Energize the aircraft electrical circuits
AMM 24-41-00-861-002.
(b) Do the EIS start procedure (Lower ECAM DU only) AMM 31-60-00-860-001.
Subtask 24-22-00-710-057-A ** ON A/C NOT FOR ALL (1) Aircraft Maintenance Configuration
(a) Energize the aircraft electrical circuits
AMM 24-41-00-861-002.
(b) Do the EIS start procedure (Lower ECAM DU only) AMM 31-60-00-860-001.
B. Test
Subtask 24-22-00-710-057-B ** ON A/C NOT FOR ALL | ACTION | RESULT |
|---|---|
1.On the ECAM control panel:
| On the lower ECAM DU:
|
| | On the lower ECAM DU:
|
| | On the lower ECAM DU:
|
B. Test
4. Fault Isolation| ACTION | RESULT |
|---|---|
1.On the ECAM control panel:
| On the lower ECAM DU:
|
| | On the lower ECAM DU:
|
| | On the lower ECAM DU:
|
Subtask 24-22-00-865-054-A
A. Make sure that this(these) circuit breaker(s) is(are) closed:
Subtask 24-22-00-810-056-A ** ON A/C NOT FOR ALL | PANEL | DESIGNATION | FIN | LOCATION |
|---|---|---|---|
| ** ON A/C NOT FOR ALL | |||
| 123VU | GEN2/EGIU2/115VAC | 23XU2 | AF01 |
B. If the test confirms the fault:
Subtask 24-22-00-810-056-B ** ON A/C NOT FOR ALL - Replace the EGIU-2 [22XU2] AMM 24-22-33-000-001 and AMM 24-22-33-400-002.
- Do a check of the position of the circuit breaker (23XU2).
- Do the procedure (Ref. TSM TASK 24-00-00-810-803).
- Replace the C/B-GEN2/EGIU2/115VAC [23XU2] .
- Do a check of the wiring ASM 242201 between:
. The pin 2 of the circuit breaker GEN2/EGIU2/115VAC (23XU2) and the pin AA/15D of the EGIU2 (22XU2)
. The pin 1 of the circuit breaker GEN2/EGIU2/115VAC (23XU2) and the pin A/D of the GLC2 (9XU2).
- Repair the wiring .
- Do a check and repair the feeder ASM 242201 between:
. The terminal T1 of the engine 2 IDG (4000XU) and the pin A/D of the GLC2 (9XU2)
. The terminal T2 of the engine 2 IDG (4000XU) and the pin A/E of the GLC2 (9XU2)
. The terminal T3 of the engine 2 IDG (4000XU) and the pin A/F of the GLC2 (9XU2).
B. If the test confirms the fault:
Subtask 24-22-00-810-056-C ** ON A/C NOT FOR ALL - Replace the EGIU-2 [22XU2] AMM 24-22-33-000-001 and AMM 24-22-33-400-002.
- Do a check of the position of the circuit breaker (23XU2).
- Do the procedure (Ref. TSM TASK 24-00-00-810-803).
- Replace the C/B-GEN2/EGIU2/115VAC [23XU2] .
- Do a check of the wiring ASM 242201 between:
. The pin 2 of the circuit breaker GEN2/EGIU2/115VAC (23XU2) and the pin AA/15D of the EGIU2 (22XU2)
. The pin 1 of the circuit breaker GEN2/EGIU2/115VAC (23XU2) and the pin 1 of the generator 2 contactor module (30XN2).
- Repair the wiring .
- Do a check and repair the feeder ASM 242201 between:
. The terminal T1 of the engine 2 IDG (4000XU) and the pin 1 of the generator 2 contactor module (30XN2)
. The terminal T2 of the engine 2 IDG (4000XU) and the pin 2 of the generator 2 contactor module (30XN2)
. The terminal T3 of the engine 2 IDG (4000XU) and the pin 3 of the generator 2 contactor module (30XN2).
B. If the test confirms the fault:
Subtask 24-22-00-810-056-F ** ON A/C NOT FOR ALL - Replace the GCU-2 [1XU2] AMM 24-22-34-000-001 and AMM 24-22-34-400-001.
- Replace the engine 2 IDG [4000XU] AMM 24-21-51-000-040 and AMM 24-21-51-400-040.
- Do a check and repair the wiring between the pins A/9, A/10 of the engine 2 IDG (4000XU) and the pins C/12, C/13 of the GCU 2 (1XU2) ASM 242201.
B. If the test confirms the fault:
Subtask 24-22-00-810-067-A ** ON A/C NOT FOR ALL - Replace GCU-2 [1XU2] AMM 24-22-34-000-001 and AMM 24-22-34-400-001.
- Replace IDG-ENG 2 [4000XU2] AMM 24-21-51-000-803 and AMM 24-21-51-400-803.
- Do a check and repair the wiring between the pins B/11, B/12 of the engine 2 IDG (4000XU) and the pins C/12, C/13 of the GCU 2 (1XU2) ASM 242201.
C. If the test confirms the fault:
Subtask 24-22-00-810-071-A ** ON A/C NOT FOR ALL - replace the EGIU-2 [22XU2] AMM 24-22-33-000-001 and AMM 24-22-33-400-002.
- do a check of the wiring between:
.the pin A/2B of the GCU2 (1XU2) and the pin A/7D of the EGIU2 (22XU2)
.the pin A/2C of the GCU2 (1XU2) and the pin A/7C of the EGIU2 (22XU2).
Then make sure that the ground wire is correctly connected to the pin A/6C of the EGIU2 (22XU2) ASM 242202.
- replace the GCU-2 [1XU2] AMM 24-22-34-000-001 and AMM 24-22-34-400-001
D. If the test confirms the fault:
Subtask 24-22-00-810-067-B ** ON A/C NOT FOR ALL - Do a check and repair the wiring ASM 315403 between:
. Pin A/1A of the EGIU2 (22XU2) and pin E/10C of the SDAC1 (1WV1)
. Pin A/1B of the EGIU2 (22XU2) and pin E/10D of the SDAC1 (1WV1)
. Pin A/1C of the EGIU2 (22XU2) and pin E/10C of the SDAC2 (1WV2)
. Pin A/1D of the EGIU2 (22XU2) and pin E/10D of the SDAC2 (1WV2)
E. If the test confirms the fault:
Subtask 24-22-00-810-071-B ** ON A/C NOT FOR ALL - replace the GCU-2 [1XU2] AMM 24-22-34-000-001 and AMM 24-22-34-400-001.
F. If the test confirms the fault:
Subtask 24-22-00-710-058-A - do a check and repair the wiring ASM 315403 between:
. the pin A/8F of the GCU 2 (1XU2) and the pin E/10C of the SDAC 1 (1WV1)
. the pin A/7F of the GCU 2 (1XU2) and the pin E/10D of the SDAC 1 (1WV1)
. the pin A/8J of the GCU 2 (1XU2) and the pin E/10C of the SDAC 2 (1WV2)
. the pin A/8H of the GCU 2 (1XU2) and the pin E/10D of the SDAC 2 (1WV2).
G. Do this test to make sure that the system operates correctly:
5. Close-up| ACTION | RESULT |
|---|---|
On the ECAM control panel:
| On the lower ECAM DU:
|
Subtask 24-22-00-860-055-A
A. Put the aircraft back to its initial configuration.
(1) Do the EIS stop procedure AMM 31-60-00-860-002.
(2) De-energize the aircraft electrical circuits
AMM 24-41-00-862-002.
(1) Do the EIS stop procedure AMM 31-60-00-860-002.
(2) De-energize the aircraft electrical circuits
AMM 24-41-00-862-002.